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Spyda's MB6 - SC before, now Turbo


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So .. Supercharger is powered by pulley instead of A/C. Pulley at A/C is 102mm, first test with original supercharger pulley, which was 92mm ;)

First ECU tuning wasn't so successfull, 1.2 PSI out of VTEC, 0.3 PSI in VTEC :evil:

imag0113ng.jpg

1) I was lookin, where should be the main problem, if piping isnt leakin'.

2) Pulley ratio is too low. ( 1:1.11 )

1. Founded some microholes, repaired... without change

2. Net calculators... ye really DONT trust em !:lol:

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Supercharger pulley was remaked, 92mm>72mm ...

Ratio was 1:1,4 .. ye there was a difference :twisted:

4PSI non VTEC , 2.7 PSI in VTEC .. not too much , but ...

First track test :) Im in category with EVO's, STI's .. my main opponents are 350z's, M3's and TT's.

1/4 mile time before supercharger - 15,303 @ 140 km/h ( 87 Mph )

1/4 mile time with supercharger (0,2bar) - 14,569 @ 159km/g ( 99Mph )

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It was near last winter, when i remaked the pulley. I really wasnt happy with the result, 4PSI :(

While i was reading a topic http://honda-tech.com/showthread.php?t=1214810&page=303 ...

founded this link http://ftlracing.com/jrsc_pulley.htm.

So i noticed, my BLOWER max rpm is 11900 ( max 6.9 PSI boost ).

Anyway im runnin supercharger oposite side then it originaly does ( H counterclock, MB clockwise ). The effectivity of this charging is 90%. A bit of pressure is also lost in pipes and IC.

New pulley :twisted:

img_20110927_175900_757.jpg

54mm diameter , so ratio is 1:1.75 :twisted:

Changed oil in blower

tmp_418_1274779498_119.jpeg 170ml of oil?

Some pictures of blower

tmp_773_89650256_207.jpeg

tmp_260222057650_181.jpeg

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Pulley is now 58mm... 6,2PSI before VTEC, 5,7PSI VTEC, aslo im runnin on E85 ( ethanol + 15% of gasoline ). Not too much, but as i want before the project starts ;)

h-2S-K-9CmQ One test :twisted:

I'll record more videos, so stay tuned :lol:

And some shots ...

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img_0117_2_270.jpg

img_0198_2_225.jpg

But suddenly after a 350km ...

img_0219_341.jpg

Maybe pulley was off-axis, so it damaged also a pulley :( Its is again remaked and its 54mm :D

Im goin to record my Bluetooth adapter, which comunicate with ECU...

JGypRgU2qgo , this program :twisted:

I'm going to change my muffler, .... so still lot of work

Maybe, ill remake the supercharger, so it will rotate like a original and the pressure will be much more :lol:

Ty for comments :!:

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